I'll start by saying that these things rock, but getting them is an utter pain in the ass. Eventually, I got these from C&R Racing in Indianapolis (Tom Keene, 317-293-4100). It seems nobody puts much useful info online to let you choose what you need, and after some frustration, I contacted Jiffy-Tite directly and they told me where to call and who to ask for. That vendor did a great job getting me what I needed, and if a part didn't work for what I needed, I could send it back for something else. Parts were drop-shipped from Jiffy-Tite. For the basic connector set (1 male/1 female straight connection) ran $36.53 for the matched set. If you need a 45 or 90-degree bend on any part rather than straight, it will cost a little bit more.
For my job, I used the 2000 series...which is the lowest level of product, but since the level is based on maximum flow rate, the 2000 series does more than a FI system will ever need. The inside diameter of the return line is 6 mm. For the supply line it is 7 mm. The same part will work for both sizes, but it was easier to get on a 7 mm line and a witch to get onto a 6 mm line. Spraying some silicone lube onto the part before working the hose on helps a lot. I used clamps on all lines although they were entirely unnecessary on the return line because they were so darn hard to get on in the first place. All Jiffy-Tite fittings are certified to 200 psi...more than enough. So long as they don't go on easily (must be a snug fit), you should need little more than a hose clamp to be assured there will be no leaks.


For this project, presuming nobody has substitutions to suggest, you will need two #22504P (male side connector), one #21504P (female side connector) and one #21504PE (female side connector w/90 degree angle).
The return line was easy, peasy lemon squeezy. I simply cut the line about 2 inches from the nipple and just put the parts on. The hardest part was getting the line onto the smaller diameter hose.


The supply line was a witch. The BIGGEST problem is that Honda gives you X inches of line and much of it bends into an S shape when the tank is down. I wound up cutting about 3 1/2 inches off the supply line so that when the tank was lowered into position, there was no undue stress on the line or any couplings. This means you have to tighten the supply line onto the rail at the last possible moment before lowering it that last inch or so onto the frame.
As you can see, I cut close to the banjo bolt...which was a mistake because it mandates a straight line from the hard bits. I made it work, but anything you do will try to put stress on this line and cutting it too close means there is no length of hose from the end of the Jiffy-Tite insert to the hard bit on the banjo bolt. If there is pressure making this bend...it's undue stress on the fuel line. I initially tried to use straight connectors, which is shorter in length, but there is no way to make it work when the tank is down without kinking the supply line. A 90-degree bend helps a lot here, and as I said, I cut about 3 1/2 inches of line off so that when it was lowered in place, there was no stress on any part of the fuel line.



The first thing you loosen and the last thing you tighten when removing/installing the tank is the nut on the supply side of the fuel rail. It needs to have play so you can get things together easily. Lift the tank up an inch or so and block up with something, use a 17 mm wrench to loosen (just enough so the banjo bolt will pivot freely), and you can then move the fuel line in a position where you can easily disconnect/connect. Just reverse when putting the tank back on.
Based on mikesail's suggestion, I replaced the worm gear clamps with fuel injection hose clamps on the high pressure line. Any auto parts store should have them, but they are SAE sized, not metric, to internal diamater. I got two different sizes and used the set sized for 5/16" I.D. hose. These worked fine. While I did screw them down all the way, I had to work at it, so I know they are good and tight. I'd recommend you go a size smaller (for 1/4" I.D. hose) so there's not all that screw shaft protruding out the other side. These defintely let you get a tighter clamp than just the worm gear style.

I wonder if a 45-degree male side connector on the fuel rail banjo bolt would have worked better here, but at most it would have made the connector easier to reach without loosening the nut on the fuel rail and perhaps cutting less excess off the fuel line.
