Hi everyone! I need some help so what better place to go than this. Hers the scoop
I have a 97 bird. I had to replace all the panels but had to do it over time. Meanwhile I got a pair of migs, a factory pro jet kit, a K&N filter and had my pipes (FI pipes by the way) Jet hot coated. Well after working with factory pro to try to get it running right I decides to go back to stock. I got a stock filter from Mike (Bartonmd)...started a new job so gonna get that to ya on friday Mike...
Anyway before I went back to stock I had 148 mains accross the four carbs and the needle clip was on the second from the bottom, pilot screw was 4 turns out from bottom. I had major cruise problems, good idle and good top end. When I closed the choke the stumble would lesson but didnt go away. I have since replace the stock filter and put the pilot screw to 3 turns out and 142 on outside carbs and 145 on inside like the european bikes are. Also put a small washer without the stock washer on the needles. It helped but the stumble is still there. I am at a loss...I feel like its running lean but I am not a carb guy...I have been working from the factory pro tuning instructions and havent solved the issue. Can anyone help me with something else to adjust or check? 29 mpg is not what I want.
Thanks
J
